emdude
Member
Finally got my motorized huffy cruiser on the road yesterday for the first time. It fired right up and once I adjusted the idle speed screw would idle fine. But WOW did my engine ever run FAT right out of the box. This thing would never stop four-stroking at all!!!. It's set up to run real rich from what I can tell. This stands to reason since I would imagine the makers don't want a seized piston within the first few miles of use. I decided to ride a bit even under these conditions and then go back home and have a look at what could be done about this.
I need to add that I live at altitude, 1600 feet to be specific and that of course doesn't help.
I also had some leaks from the carb, one was due to a loose float needle seat and the other from a not all to good seal of the float bowl. Got those items taken care of.
Another thing that indicated really rich mixture was the old "shut off the fuel and see what happens" trick. So I shut off the fuel supply on a long straight away and sure enough power picked up for a brief moment just before the engine shut off. This increased my confidence in assuming the engine was running way too rich.
So in examining the supper richness of the engines running I tried the following:
First I ran it with out the air cleaner just to see if this made any difference. Nothing of note here, seems this flows enough.
After that I lowered the jet needle to its lowest position and lowered the float level. The float level seems to be suspiciously high. This made a major improvement. Most of the four stroking was now gone. I could get up most hills in my area with out having to help it along by pedaling.
Of course it still four stroked at higher RPMs which I would sort of expect. Most small engines like this do because it reaches a point at which the exhaust is the limiting factor. It just won't let enough out anymore. Actually this can be caused by pretty much anything, not enough getting out, not enough getting in, or even any not ideal timing event including transfer ports. I did think it was the exhaust though in my case.
Then I removed the end of the exhaust. And that made all the difference!!!. Plenty of noise of course and no more four stroking at all. It really picked up and went at all RPMs. There's a lot being lost in the EPA exhaust that came with my engine.
I'm going to work on getting the mixture as right as I can get it and if I find anything noteworthy will report.
In my first post I had described how I had a close look at my engine before ever installing it. I had found that on my engine the cylinder base gasket was not cut all that well and was quite substantially covering the transfer ports. I had decided too leave it alone, which I now regret. This could be quite a limitation after all. I may have to take the engine out get this cleaned up just to be sure I'm not taking a hit here.
Udate:
I went home for lunch today, after writing the above earlier this morning and tried to start the bike. It's fairly cold here so I set the choke. No deal, would not run. Started right away with the choke turned fully off. Another indication of a rich mixture.
Regards
emdude
I need to add that I live at altitude, 1600 feet to be specific and that of course doesn't help.
I also had some leaks from the carb, one was due to a loose float needle seat and the other from a not all to good seal of the float bowl. Got those items taken care of.
Another thing that indicated really rich mixture was the old "shut off the fuel and see what happens" trick. So I shut off the fuel supply on a long straight away and sure enough power picked up for a brief moment just before the engine shut off. This increased my confidence in assuming the engine was running way too rich.
So in examining the supper richness of the engines running I tried the following:
First I ran it with out the air cleaner just to see if this made any difference. Nothing of note here, seems this flows enough.
After that I lowered the jet needle to its lowest position and lowered the float level. The float level seems to be suspiciously high. This made a major improvement. Most of the four stroking was now gone. I could get up most hills in my area with out having to help it along by pedaling.
Of course it still four stroked at higher RPMs which I would sort of expect. Most small engines like this do because it reaches a point at which the exhaust is the limiting factor. It just won't let enough out anymore. Actually this can be caused by pretty much anything, not enough getting out, not enough getting in, or even any not ideal timing event including transfer ports. I did think it was the exhaust though in my case.
Then I removed the end of the exhaust. And that made all the difference!!!. Plenty of noise of course and no more four stroking at all. It really picked up and went at all RPMs. There's a lot being lost in the EPA exhaust that came with my engine.
I'm going to work on getting the mixture as right as I can get it and if I find anything noteworthy will report.
In my first post I had described how I had a close look at my engine before ever installing it. I had found that on my engine the cylinder base gasket was not cut all that well and was quite substantially covering the transfer ports. I had decided too leave it alone, which I now regret. This could be quite a limitation after all. I may have to take the engine out get this cleaned up just to be sure I'm not taking a hit here.
Udate:
I went home for lunch today, after writing the above earlier this morning and tried to start the bike. It's fairly cold here so I set the choke. No deal, would not run. Started right away with the choke turned fully off. Another indication of a rich mixture.
Regards
emdude
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