(about the milling machine)... I had my eye on Harbor Freight's mini-mill for a while, but found one used on Craigslist for $350 (reg. $600). He even threw in 6 different sized collets, so I got lucky on that one. Here's the link to it.....
http://www.harborfreight.com/cpi/ctaf/displayitem.taf?Itemnumber=44991
But anyway, man I hope my second one IS easier than the first (many mistakes made). The main mistake, despite my best effort, misaligned the two large 1- 3/16" holes for the roller drive (drilled out with a step-bit). It was off just a hair, enough to make the drive noticeably uneven. I felt that it might put an extra strain on the engine if left that way, so I shaved of more aluminum on side to even it up. But that caused some slack around the 1-3/16" bearing, making it shake around and vibrate real bad. So I used layers upon layers of aluminum tape (leftover from some duct work a while back), and filled in the gap. So now, both bearings are snug and even steven.
The clutch drum sticking was partly because the 5" long shoulder bolt (1/2" width, 3/16" threads , then screwed into the clutch drum) was pressing into the tension spring between the centrifugal clutch's flyweights. Also partly because of the bearing issue. So after fixing that, I milled about 1/2" off the threaded part, put it back together and PROBLEM RESOLVED. Wooo hooo.
thanks for the words and thoughts!! I really like this forum.
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http://www.harborfreight.com/cpi/ctaf/displayitem.taf?Itemnumber=44991
But anyway, man I hope my second one IS easier than the first (many mistakes made). The main mistake, despite my best effort, misaligned the two large 1- 3/16" holes for the roller drive (drilled out with a step-bit). It was off just a hair, enough to make the drive noticeably uneven. I felt that it might put an extra strain on the engine if left that way, so I shaved of more aluminum on side to even it up. But that caused some slack around the 1-3/16" bearing, making it shake around and vibrate real bad. So I used layers upon layers of aluminum tape (leftover from some duct work a while back), and filled in the gap. So now, both bearings are snug and even steven.
The clutch drum sticking was partly because the 5" long shoulder bolt (1/2" width, 3/16" threads , then screwed into the clutch drum) was pressing into the tension spring between the centrifugal clutch's flyweights. Also partly because of the bearing issue. So after fixing that, I milled about 1/2" off the threaded part, put it back together and PROBLEM RESOLVED. Wooo hooo.
thanks for the words and thoughts!! I really like this forum.
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