phatmotocat
Member
So the next issue I ran into was the new carburetor. The idle was good but it would konk on throttle. I examined the main jet and noticed whoever installed it made a mess of the jet and particles of brass left to partly block the hole. After cleaning and testing the bike ran much better but I can tell it is still under jet size after drilling to .69 Have a jet kit on order so I should be able to get better performance than the current 60kph or 40 mile and hour. Have many budget performance upgrades to come.With the way you did the engine riser you might be able to get away with moving the engine over a bit to help with alignment. If that's not possible, you might be able to space the driven pulley over to lighn up better.