James Owens
New Member
- Local time
- 1:26 AM
- Joined
- Oct 20, 2017
- Messages
- 12
So I accidentally destroyed my last motor and ended up getting a new one a couple days ago. I ended up exchanging just the motor and used pretty much all of the old components. The old motor was working fantastic before I broke it (stripped head stud holes, then stripped the helicoils). After getting everything assembled, the new motor was running piss poor. It will idle, but once the clutch is engaged it has very little power (cant go up any inclines without having to pedal assist, top speed on flat ground at WOT only around 15-20mph.) It seems to be fourstroking, but I'm not entirely positive on that.
I first thought it was something electrical that was the problem as I got sloppy with the wiring. I then replaced the kill switch, magneto, and CDI. Problem persisted.
I then replaced the spark plug with a b6hs and the problem still persisted.
I then took the air filter off the carb to see if it was restricting the airflow. Still had the problem without the filter.
I then swapped the carb out for a different one. Still had the problem.
Adjusting c-clip also seemed to do nothing.
The exhaust is super smokey and the plug looked wet with oil after all this testing so I assume it must be running way too rich. I just don't understand why, as both of my carbs worked great on the old motor with the same jets.
I don't see any sort of gasket leaks, but my second guess is a loss of compression due to the problem being only while the motor is under load.
Next I guess I will swap out the muffler in case it's clogged, but the muffler I'm using had less than 100 miles on it running 1:32 full synthetic, so I doubt it's clogged.
The only other thing I can think to do is just port and polish it and trim the piston skirt to get better flow, but I doubt it will help.
Any ideas or suggestions? I'm more or less at a loss
I first thought it was something electrical that was the problem as I got sloppy with the wiring. I then replaced the kill switch, magneto, and CDI. Problem persisted.
I then replaced the spark plug with a b6hs and the problem still persisted.
I then took the air filter off the carb to see if it was restricting the airflow. Still had the problem without the filter.
I then swapped the carb out for a different one. Still had the problem.
Adjusting c-clip also seemed to do nothing.
The exhaust is super smokey and the plug looked wet with oil after all this testing so I assume it must be running way too rich. I just don't understand why, as both of my carbs worked great on the old motor with the same jets.
I don't see any sort of gasket leaks, but my second guess is a loss of compression due to the problem being only while the motor is under load.
Next I guess I will swap out the muffler in case it's clogged, but the muffler I'm using had less than 100 miles on it running 1:32 full synthetic, so I doubt it's clogged.
The only other thing I can think to do is just port and polish it and trim the piston skirt to get better flow, but I doubt it will help.
Any ideas or suggestions? I'm more or less at a loss